Fuckin blown moter's
****** blown moter's
Well the dreaded number 4 bit me in the ass. I am stock with a zex 50 shot (wet) Damn thing has been running good and all of a sudden the idle went to ****. Took the car to the shop checked my plugs they were fine. Went out for another run sprayed a few times then came back to the shop. My friend goes , why is your car smoking? So i lift the hood and there is oil everywhere, dipstick poped out. Well i did a compression test and found that cylinder 1,2,3 had 160 lbs and 4 was 60 lbs. I have been driving the car around still runs ok idle is a little off.
I am pretty sure i screwed the piston but is there a chance that it can be the valves?
There is no smoke out the tailpipe car still has good acceleration.
Yes i know i mispelled motor
I am pretty sure i screwed the piston but is there a chance that it can be the valves?
There is no smoke out the tailpipe car still has good acceleration.
Yes i know i mispelled motor
apparently, if you're setup is correct, you shouldnt have issues with a 50 wet and being stock...thats a huge IF though, hence my cancelation of my order of a zex wet 50 during xmas...had second thoughts ....
hope your car is ok man
hope your car is ok man
I ran that shot for year and a half with no problems. I tapped the plastic just before the throttle body and sprayed through the sc, I cannot remember which wire i tapped into for the tps signal but will check later.
I was doing a little checking and found that the nitrous nozzle i went to had been drilled from a previous drag car setup we had. Thought we threw it away.
oh well ran good for awhile, according to the zex tech guy i was spraying 125 shot.
I was doing a little checking and found that the nitrous nozzle i went to had been drilled from a previous drag car setup we had. Thought we threw it away.
oh well ran good for awhile, according to the zex tech guy i was spraying 125 shot.
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shawnsseries
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Sep 10, 2015 08:29 PM




