ppl with zzp turbo setup
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From: troy,michigan
Kk sweet I just waiting for Vince to call me back the damn tune he sent me won't upload and of course he's not anserwing the phone
Oh yea and the dp is hugeee it dosnt even come close to mounting up to my Megan racing catback
i need help with the waste gate do u run the one vacum line in the top and one in the side its a tial wastegate is that helps
Oh yea and the dp is hugeee it dosnt even come close to mounting up to my Megan racing catback
i need help with the waste gate do u run the one vacum line in the top and one in the side its a tial wastegate is that helps
Last edited by mmcgee123; Mar 3, 2010 at 02:30 PM. Reason: Automerged Doublepost
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From: troy,michigan
i kno that it still have to lines goin to the wastegate and im just wondering how to run them cus theres two holes in the cap and then three around the base of the cap on the acauly wastegate and the kit came with 3 allen bolts i have both the lines running into the cap right now but i have a feiling one of them needs to go into the lower part of the wastegate zzp didnt give any instructions on thsi
Figured it out car runs ok it's driveable me n Vince are still workin on it alota data logs it breaks up pretty good when u give it over 1/2 throttle
Figured it out car runs ok it's driveable me n Vince are still workin on it alota data logs it breaks up pretty good when u give it over 1/2 throttle
Last edited by mmcgee123; Mar 3, 2010 at 08:35 PM. Reason: Automerged Doublepost
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From: troy,michigan
Update car runs amazing runnin about 8 psi right now throws a too rich code and a idle speed high code pulls hard right now tho I'm gettin my exhaust made tomarrow to fit thus huge ass down pipe
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From: troy,michigan
Update got the exhaust fixed it sounds amzing were still gettin kr and I'm only at 8-9 psi I think were only running 8* of timing this motor is not really liking boost right now ha
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From: troy,michigan
mid 11's low 12 on 91 octane the best we can get in az besides race gas
i dont get waht the issue is here timing isnt a issue fuel is pretty much alrite and the false knock is gone
i dont get waht the issue is here timing isnt a issue fuel is pretty much alrite and the false knock is gone
i dont get waht the issue is here timing isnt a issue fuel is pretty much alrite and the false knock is gone
i dont get waht the issue is here timing isnt a issue fuel is pretty much alrite and the false knock is gone
Last edited by mmcgee123; Mar 6, 2010 at 05:28 PM. Reason: Automerged Doublepost
mid 11's low 12 on 91 octane the best we can get in az besides race gas
i dont get waht the issue is here timing isnt a issue fuel is pretty much alrite and the false knock is gone
i dont get waht the issue is here timing isnt a issue fuel is pretty much alrite and the false knock is gone
i dont get waht the issue is here timing isnt a issue fuel is pretty much alrite and the false knock is gone
i dont get waht the issue is here timing isnt a issue fuel is pretty much alrite and the false knock is gone
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From: troy,michigan
we got everything settled for now im only running 9psi at the moment were goin to the track saturday night im pretty excited to see how she does when i had 100 shot full boltons and a tune best it went was 13.6@109 and this thing only on 9psi feils wayyy wayyyyy faster then before
we got everything settled for now im only running 9psi at the moment were goin to the track saturday night im pretty excited to see how she does when i had 100 shot full boltons and a tune best it went was 13.6@109 and this thing only on 9psi feils wayyy wayyyyy faster then before
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From: troy,michigan
Update went to the track on 9 psi I ran a 13.73 @ 104.8 2.36-60ft I m on bfg dragradials runnin 18psi had to feather the throttle thru first and second nooo traction I guess it's time for slicks and more boost ha
Oh yea and when it hits second gear and pops and shoots a nice flame ha
Oh yea and when it hits second gear and pops and shoots a nice flame ha
Last edited by mmcgee123; Mar 14, 2010 at 03:06 AM. Reason: Automerged Doublepost


