Marylanders R calling You OUT!
#6628
Senior Member
iTrader: (2)
Join Date: 10-12-07
Location: Essex, MD
Posts: 3,306
Likes: 0
Received 0 Likes
on
0 Posts
...eventually
it was comical hearing some of the off-the-wall **** you were guessing at saturday night lmfao
it was comical hearing some of the off-the-wall **** you were guessing at saturday night lmfao
Last edited by bobbyhill31286; 04-06-2011 at 06:54 PM. Reason: Automerged Doublepost
#6631
Senior Member
iTrader: (4)
Join Date: 07-23-07
Location: cordova, Maryland
Posts: 1,706
Likes: 0
Received 0 Likes
on
0 Posts
yea yea glad to hear bout the radio and the engine is all done just waiting on one cooling hose that got effed up it will be tomorrow, debating on stealing oscar's wheels for the nite just to see how they look
#6634
Senior Member
Join Date: 09-08-08
Location: Maryland
Posts: 21,994
Likes: 0
Received 0 Likes
on
0 Posts
#6644
Senior Member
iTrader: (2)
Join Date: 10-12-07
Location: Essex, MD
Posts: 3,306
Likes: 0
Received 0 Likes
on
0 Posts
Im still waiting for a damn tracking # from ottp for the pipes. I just tried logging into their site and nothing is happening. it keeps taking me back to the logon screen (i know i entered my email and password right). I just sent them an email to try and find out what is going on. Paypal shows that they have gotten payment from me and still...nothing.
Pretty sad that i am getting pads/rotors from califormia quicker than i can get damn pipes from michigan
Pretty sad that i am getting pads/rotors from califormia quicker than i can get damn pipes from michigan
#6648
Senior Member
iTrader: (3)
Join Date: 05-18-10
Location: Calvert County MD
Posts: 891
Likes: 0
Received 0 Likes
on
0 Posts
so for anyone who has been following my problem(s)... heres a little story... about 2 weeks ago my shifter became sloppy as hell and i also was unable to quickly shift to gear 2 and 4... i was like **** this is gonna cost alot of money... i didnt no what the problem was i thought it was synchros thouhght it was linkages though it was a fork thuoght it was a clutch rod.... so to the rescue comes Countryss who nicely provides some services and was gonna take care of me... well i started reading up on roll pins and i was like well hell i should at least try this before i make someone else waste all their time for only a roll pin.. so i take the fuse box out and all that ****.. get it out and i cant get the ******* roll pin out bc of the angles and lack of tools for the job... so i was like **** it but i looked around down by the linkages and stuff and noticed that a bolt was only about halfway tightedned where i could see about 5 threads... i wasnt sure if this should be like this because it was on a pivoted mechanism but i tightened it anyway for fun... put the ******* car back together and say well i mise well drive it to make sure i didnt **** anythign up... shifter is the tightest its ever been.. and i was like well ****.. so i stop.. and decide to see how it likes the 1-2 shift... it likes it more than ever... so basically this rant is bc of all the things that could have and should have gone wrong the problem was a loose ******* bolt... and for anyone who wants to tighten their shifts a bit this is the bolt to use... i dont have a picture but i could point it out... so now im happy again and can go back to driving like a dick...