2.0L LNF Performance Tech 260hp and 260 lb-ft of torque Turbocharged tuner version.

another no boost issue

Old Jul 27, 2012 | 01:25 PM
  #26  
SSlobalt's Avatar
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From: Kathmandu
OP, do you have a metal aftermarket intake? Also, if you do not, is that rectangular gasket around the MAF still present and undamaged?

If you want to try a new MAF, monograt has a ton of them for sale, and cheap.
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Old Jul 30, 2012 | 08:40 PM
  #27  
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From: Winston Salem, NC
i have tried 3 brand new mafs. all the same, i have a injen intake. and the rubber square gasket is still present. i almost think its cuz of the boost control sensor. i had the code set to OFF since i deleted it and then we retuned for the maf cuz it was 10% out of wack.

previous tune had the p0033 turned off with my hptuners. but i sold mine and had to use his and he did not have it turned off in his hpt. since p0033 is a type b code (drivability code) i feel like thats it. but i have no clue until i can get with him
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Old Jul 30, 2012 | 11:21 PM
  #28  
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From: Kathmandu
Why are you not using your BPV solenoid?
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Old Aug 1, 2012 | 08:50 AM
  #29  
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From: Winston Salem, NC
when i removed the vacuum tank i removed the sensor and just ran the bpv vac line straight to the manifold. slightly quicker response from th bpv when closed throttle and slightly quicker spool. if anything it just ran more smoothly.

but im not convinced thats the reason for my issues. im almost certain its the maf is just way out of range,
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Old Aug 1, 2012 | 10:03 PM
  #30  
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From: Kathmandu
Originally Posted by sprchrgdss
when i removed the vacuum tank i removed the sensor and just ran the bpv vac line straight to the manifold. slightly quicker response from th bpv when closed throttle and slightly quicker spool. if anything it just ran more smoothly.

but im not convinced thats the reason for my issues. im almost certain its the maf is just way out of range,
Can you log?
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Old Aug 3, 2012 | 01:24 PM
  #31  
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From: Winston Salem, NC
logged today, maf was going to - 30. corrected it then went +30. put an old tune on it and seems to be running ok now, so we shal drive and see what happens
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Old Aug 3, 2012 | 01:32 PM
  #32  
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From: Kathmandu
Good to hear. Fuel trim issue.
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Old Aug 6, 2012 | 06:41 PM
  #33  
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From: Oklahoma City
Keep updated! I'm having the same problem with p0101 and its not a boost leak. I plan on checking wiring today to see if there is a break in a wire somewhere.
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Old Aug 7, 2012 | 08:11 AM
  #34  
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Yeah, I'm getting the P0101 as well (along with P0106 and P0236) and I did a boost leak test to 26 psi the other day and couldn't hear any hissing whatsoever so I don't think my issue is a boost leak either.

I will say though that I have the K&N SRI and it doesn't look like there's a gasket or anything sealing the face of the sensor to the face on the intake.
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Old Aug 8, 2012 | 09:35 PM
  #35  
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Originally Posted by DPveritasGold
Yeah, I'm getting the P0101 as well (along with P0106 and P0236) and I did a boost leak test to 26 psi the other day and couldn't hear any hissing whatsoever so I don't think my issue is a boost leak either.

I will say though that I have the K&N SRI and it doesn't look like there's a gasket or anything sealing the face of the sensor to the face on the intake.
I have been getting the same codes and dont have a boost leak, I am going to get a retune even tho I dont think that will help.
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