2.4L LE5 Performance Tech 16 valve 171 hp EcoTec with 163 lb-ft of torque

2.4ss/sc build commenced!!!

Thread Tools
 
Search this Thread
 
Old May 23, 2009 | 02:54 AM
  #301  
Dragonsfire12345's Avatar
Thread Starter
Senior Member
iTrader: (1)
 
Joined: 11-01-05
Posts: 5,435
Likes: 0
From: San Antonio,TX
lol its a stock pulley, and stock intake.... gonna get a cai asap. exhaust is zzp shortie header, stock dp minus cat, and borla muffler

oh and after I recorded that little preview.... my wideband stopped reading.

Last edited by Dragonsfire12345; May 23, 2009 at 02:54 AM. Reason: Automerged Doublepost
Reply
Old May 23, 2009 | 03:09 AM
  #302  
elecblue06's Avatar
Senior Member
iTrader: (1)
 
Joined: 03-19-07
Posts: 14,901
Likes: 1
From: newburgh,ny
Originally Posted by Dragonsfire12345
lol its a stock pulley, and stock intake.... gonna get a cai asap. exhaust is zzp shortie header, stock dp minus cat, and borla muffler

oh and after I recorded that little preview.... my wideband stopped reading.
ahh ok so that explains it lol free up that exhaust and intake a bit more and it'll scoot lol


that sucks about the wideband what brand?
Reply
Old May 23, 2009 | 03:10 AM
  #303  
Dragonsfire12345's Avatar
Thread Starter
Senior Member
iTrader: (1)
 
Joined: 11-01-05
Posts: 5,435
Likes: 0
From: San Antonio,TX
innovative
Reply
Old May 23, 2009 | 05:52 AM
  #304  
Jn2's Avatar
Jn2
Senior Member
iTrader: (1)
 
Joined: 05-04-07
Posts: 7,791
Likes: 3
From: Texas
Did it hit 7.4 and stay that way? That's normal, it will happens after long wot pulls like during tuning, u overheated the o2 sensor, I called innovate in it, check ur instructions it tells u what to do if ur egt's go higher than the sensor will allow

also if u can wait till July I'll sell u by knn intake, I'll be upgrading to a zzp 3" on later in late June, also I'll see u my lsj throttle body if you want, I'm getting a ls4 one in June aswell

Last edited by Jn2; May 23, 2009 at 05:52 AM. Reason: Automerged Doublepost
Reply
Old May 23, 2009 | 11:51 AM
  #305  
Dragonsfire12345's Avatar
Thread Starter
Senior Member
iTrader: (1)
 
Joined: 11-01-05
Posts: 5,435
Likes: 0
From: San Antonio,TX
yeah I guess thats what I did lol..... Having to much fun driving around last night. I'm just gonna wait and get a 3in intake, ls4. At the same time, figure I just save up and buy that stuff right off the bat instead of spending money on other stuff and then just selling it.

On another note I can't find in the manual where it says what to do

Last edited by Dragonsfire12345; May 23, 2009 at 12:28 PM.
Reply
Old May 23, 2009 | 01:35 PM
  #306  
rico's Avatar
Senior Member
 
Joined: 12-09-07
Posts: 8,962
Likes: 0
From: San Antonio, TX
damn jo jo i wanna see the car lol
Reply
Old May 23, 2009 | 02:05 PM
  #307  
Dragonsfire12345's Avatar
Thread Starter
Senior Member
iTrader: (1)
 
Joined: 11-01-05
Posts: 5,435
Likes: 0
From: San Antonio,TX
lol reason why car is running lean at idle, and rich at wot is due to the bank 1 o2 sensor Its dead
Reply
Old May 23, 2009 | 03:21 PM
  #308  
Zdeuce4's Avatar
Senior Member
iTrader: (1)
 
Joined: 12-16-07
Posts: 4,441
Likes: 0
From: S.A
Originally Posted by Dragonsfire12345
lol reason why car is running lean at idle, and rich at wot is due to the bank 1 o2 sensor Its dead
im sick of all the fail...fix it!!!
Reply
Old May 23, 2009 | 08:34 PM
  #309  
Jn2's Avatar
Jn2
Senior Member
iTrader: (1)
 
Joined: 05-04-07
Posts: 7,791
Likes: 3
From: Texas
Originally Posted by Zdeuce4
im sick of all the fail...fix it!!!
Reply
Old May 23, 2009 | 09:17 PM
  #310  
HunterKiller89's Avatar
Senior Member
iTrader: (1)
 
Joined: 07-20-06
Posts: 11,183
Likes: 4
From: Los Angeles
Originally Posted by Zdeuce4
im sick of all the fail...fix it!!!
qft!
Reply
Old May 23, 2009 | 10:39 PM
  #311  
Dragonsfire12345's Avatar
Thread Starter
Senior Member
iTrader: (1)
 
Joined: 11-01-05
Posts: 5,435
Likes: 0
From: San Antonio,TX
so I replaced the o2 sensor, cleared the codes with the trifecta tuner. Then turned car off and turned it back on and its still there.
Reply
Old May 23, 2009 | 11:05 PM
  #312  
BULLETSSMOKE's Avatar
Senior Member
 
Joined: 10-31-07
Posts: 2,765
Likes: 1
From: Houston, TX
would anyone be kind to point me in the right direction for this 2.4SC project. looks like fun and ive wanted to be supercharged for a while. the project doesnt seem too hard from what ive seen.
Reply
Old May 24, 2009 | 12:57 AM
  #313  
Dragonsfire12345's Avatar
Thread Starter
Senior Member
iTrader: (1)
 
Joined: 11-01-05
Posts: 5,435
Likes: 0
From: San Antonio,TX
oh forgot to say the code is p0171

here is a vid of the car at idle
http://www.youtube.com/watch?v=VYOJKAn9-VI

Last edited by Dragonsfire12345; May 24, 2009 at 12:58 AM. Reason: Automerged Doublepost
Reply
Old May 24, 2009 | 02:27 AM
  #314  
HunterKiller89's Avatar
Senior Member
iTrader: (1)
 
Joined: 07-20-06
Posts: 11,183
Likes: 4
From: Los Angeles
sounds like a MAF issue to me. Everything is installed fine, right? MAF isnt backwards or anything? Wires are all good? Try swapping the sensor itself out for one you know works perfectly and see what you get
Reply
Old May 24, 2009 | 11:09 AM
  #315  
Dragonsfire12345's Avatar
Thread Starter
Senior Member
iTrader: (1)
 
Joined: 11-01-05
Posts: 5,435
Likes: 0
From: San Antonio,TX
the maf is dummy proof only installs one way. Maybe it got dirty, how can I clean it.
Reply
Old May 24, 2009 | 11:47 AM
  #316  
glen229's Avatar
Senior Member
iTrader: (4)
 
Joined: 06-20-08
Posts: 6,173
Likes: 1
From: S. Easton, Ma
MAF cleaner at autozone
Reply
Old May 24, 2009 | 03:51 PM
  #317  
HunterKiller89's Avatar
Senior Member
iTrader: (1)
 
Joined: 07-20-06
Posts: 11,183
Likes: 4
From: Los Angeles
Originally Posted by Dragonsfire12345
the maf is dummy proof only installs one way. Maybe it got dirty, how can I clean it.
i knew of one member who (somehow) managed to install it backwards and it was causing MAF issues. I didnt bother asking how he managed to do that, but since then, ive always included it in my troubleshooting list of things to check..lol
Reply
Old May 24, 2009 | 06:22 PM
  #318  
Dragonsfire12345's Avatar
Thread Starter
Senior Member
iTrader: (1)
 
Joined: 11-01-05
Posts: 5,435
Likes: 0
From: San Antonio,TX
found the problem... it appears that the intake manifold is still leaking on one side. The bolts are tightened down and torqued to specs. We believe the intake manifold is warped. When you put it on, one side would sit flush on the head while the other side doesn't even rest on the other side.
Reply
Old May 24, 2009 | 06:43 PM
  #319  
rico's Avatar
Senior Member
 
Joined: 12-09-07
Posts: 8,962
Likes: 0
From: San Antonio, TX
wtf gayy. man **** and i though u was all good now damn
Reply
Old May 24, 2009 | 07:10 PM
  #320  
Dragonsfire12345's Avatar
Thread Starter
Senior Member
iTrader: (1)
 
Joined: 11-01-05
Posts: 5,435
Likes: 0
From: San Antonio,TX
it is good, just a very small leak.... so the car is not running 100%
Reply
Old May 24, 2009 | 07:34 PM
  #321  
HunterKiller89's Avatar
Senior Member
iTrader: (1)
 
Joined: 07-20-06
Posts: 11,183
Likes: 4
From: Los Angeles
double gasket as a temporary fix maybe?
Reply
Old May 24, 2009 | 08:02 PM
  #322  
rico's Avatar
Senior Member
 
Joined: 12-09-07
Posts: 8,962
Likes: 0
From: San Antonio, TX
ah okay good and ya mayb what hunter said will help
Reply
Old May 24, 2009 | 08:29 PM
  #323  
Dragonsfire12345's Avatar
Thread Starter
Senior Member
iTrader: (1)
 
Joined: 11-01-05
Posts: 5,435
Likes: 0
From: San Antonio,TX
good idea but I threw away the old gasket
Reply
Old May 24, 2009 | 08:36 PM
  #324  
rico's Avatar
Senior Member
 
Joined: 12-09-07
Posts: 8,962
Likes: 0
From: San Antonio, TX
ah damn u lol. buy another one? lol
Reply
Old May 24, 2009 | 08:47 PM
  #325  
Dragonsfire12345's Avatar
Thread Starter
Senior Member
iTrader: (1)
 
Joined: 11-01-05
Posts: 5,435
Likes: 0
From: San Antonio,TX
by the time it takes to come I could have already taken off the intake manifold and gone to the machine shop to have it leveled.
Reply



All times are GMT -4. The time now is 09:15 PM.